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Sunbird Photos by Don Boyd | all galleries >> Civil Aircraft Stock Photo Galleries sorted by AIRCRAFT TYPE - AviationStockPhotos.com >> Boeing B727 Stock Photos Gallery - AviationStockPhotos.com > 1982 - #2 engine fire on Pan Am B727-235 N4734 stock photo
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17-FEB-1982 ©1982 Don Boyd

1982 - #2 engine fire on Pan Am B727-235 N4734 stock photo

Runway 30, Miami International Airport


Flight 975 to Orlando was starting its takeoff roll on runway 27-left when the front compressor hub failed and severed the main fuel line in the #2 engine which spewed fuel that ignited. The crew turned onto runway 30 and stopped quickly to evacuate the passengers. The passengers evacuated safely with no fatalities and the ARFF extinguished the fire quickly.

From: http://www.ntsb.gov/ntsb/brief.asp?ev_id=20020917X02404&key=1

NTSB Identification: MIA82FA051
Scheduled 14 CFR Part 121: Air Carrier operation of PAN AMERICAN WORLD AIRWAYS, IN
Accident occurred Wednesday, February 17, 1982 in MIAMI, FL
Probable Cause Approval Date: 2/17/1983
Aircraft: BOEING 727-235, registration: N4734
Injuries: 1 Serious, 1 Minor, 51 Uninjured.

DURING TAKEOFF ROLL A LOUD BANG WAS HEARD & THE TAKEOFF ABORTED. THE TOWER ADVISED THE FLT OF EXTENSIVE FIRE IN THE TAIL AREA. THE PLT CLEARED THE ACTIVE RWY & THE ACFT WAS EVACUATED. 1 PAX SUFFERED A FRACTURED ANKLE & ANOTHER A SPRAINED ANKLE. AN EXPLOSION HAD OCCURRED IN THE #2 ENG DUE TO A FAILED FRONT COMPRESSOR FRONT HUB. THE MAIN FUEL SUPPLY LINE TO THE #2 ENG WAS SEVERED CAUSING THE FIRE. METALLURGICAL EXAMINATION REVEALED THAT THE HUB FRACTURED RADIALLY THROUGH THE BORE & RIM IN TWO LOCATIONS RELEASING TWO SECTIONS. FATIGUE HAD ORIGINATED AT A NONCONFORMING CIRCUMFERENTIAL GROOVE AT THE REAR OF ONE TIE ROD HOLE. THE SURFACE OF THE GROOVE EXHIBITED A VERY ROUGH, SMEARED APPEARANCE & THERE WERE NUMEROUS AXIAL CRACKS.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows: COMPRESSOR ASSEMBLY..FATIGUE, COMPRESSOR ASSEMBLY..FAILURE,TOTAL

Contributing Factors: INADEQUATE QUALITY CONTROL..MANUFACTURER


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